Preparation of an Environmental Impact
Statement for construction, operation and
deactivation of a proposed Mixed Oxide Fuel
Fabrication Facility to be constructed at the
Department of Energys Savannah River Site
in South Carolina
BLUE RIDGE ENVIRONMENTAL DEFENSE LEAGUE
www.BREDL.org
~ PO Box 88 Glendale Springs, North Carolina
28629 ~ Phone (336) 982-2691 ~ Fax (336) 982-2954
~ BREDL@skybest.com
May 8, 2001
Mike Lesar, Chief,
Rules and Directives Branch
Division of
Administrative Services
Office of
Administration
Mail Stop T6D59
U.S. Nuclear
Regulatory Commission,
Washington DC
20555.
Re: Docket
70-3098, Preparation of an Environmental Impact
Statement for construction, operation and
deactivation of a proposed Mixed Oxide Fuel
Fabrication Facility to be constructed at the
Department of Energys Savannah River Site
in South Carolina
Dear Sir:
I write to provide
additional comments on the proposed MFFF. This
letter will focus on nuclear reactor safety
issues with regards to fuel made from
weapons-grade plutonium.
The planned use of
mixed oxide (MOX) plutonium fuel is unsafe,
uneconomical, and unnecessary. We oppose the use
of plutonium fuel in commercial power reactors
for the following reasons:
Plutonium
fuel derived from dismantled weapons is
an experimental program which cannot be
compared to European experience with
plutonium fuel made from nuclear waste.
The mix of isotopes includes 64% higher
concentration of Plutonium 239, the heart
of a nuclear weapon. Safety hazards in
nuclear plants are a combination of human
and technical errors. Both types of error
are noted in the Nuclear Regulatory
Commissions Plant Performance
Reviews of the McGuire and Catawba
reactors (see Attachment). Because of the
inherent hazards in these plants, DOE
should not move forward with the MOX
plan.
The
Catawba and McGuire plants operated by
Duke have a radiation containment
building which depends on blocks of ice
to reduce heat and pressure in case of a
reactor accident. Dukes ice
condenser system has inherent weaknesses
which have resulted in safety problems
and lengthy closures of other utility
reactors using the same system.
The
Department of Energys selection of
DCS and the planned utilization of Duke
Power reactors have not been opened to
full public scrutiny. The experimental
nature of a weapons-derived fuel project
requires a thorough and independent
assessment by NRC. Additional information
from DOE and DCS is required to fully
assess the safety of this program.
The
planned use of plutonium fuel in the
reactors operated by Duke Power would be
a dangerous precedent in the domestic
nuclear industry, needlessly exposing
many people to the risk of additional
radiation exposure from a plutonium
fuel-powered plant accident. Furthermore,
the use of plutonium fuel in commercial
reactors is a break with two decades of
American non-proliferation policy and
opens a door for other nations to exploit
for the purpose of plutonium weapons
production.
Plutonium Fueled Reactor Hazards
Commercial
Nuclear Reactors Were Not Designed for Plutonium
Fuel
Atom splitting in
a reactor releases neutrons which split other
atoms. This chain reaction is what drives the
reactor. The chain reaction must be precisely
controlled in order to produce power safely.
Compared to neutrons from uranium atoms,
plutonium releases more neutrons at a higher
speed and energy during the fission process.
Technical
issues that arise in the analysis of risk
at plants using MOX focus on the
vulnerability of fuel to neutronically
induced core disruption and the different
inventory of radionuclides available for
release from the fuel during accidents.
The differences in neutronics and
coupling between neutronics and thermal
hydraulics result in different responses
of MOX and conventional fuel to
reactivity transients. May
17, 1999 letter to NRC Chairman from the
Chair of the Advisory Committee on
Reactor Safeguards
Adding
plutonium to the reactor in the form of MOX
reduces the ability to control the chain
reaction:
The rate
of fission in plutonium increases with
temperature, and the problem is greater
with MOX fuel made from weapons-grade
plutonium. MOX fuel in a reactor attains
higher temperatures than uranium fuel
because of the higher quantity of
transuranic elements produced during
irradiation. The percentage of delayed
neutrons emitted seconds to minutes after
a plutonium atom splits is just one-third
that of uranium (Pu239=0.2%, U235=0.65%).
This means plutonium releases a higher
amount of its neutrons in a single burst
and adds to reactor control problems.
Plutonium
captures more neutrons than uranium,
increasing fission and making control
measures less effective.
~Institute for Energy and
Environmental Research, SDA February 1997
Experience
With Plutonium Fuel In The U.S. Is Limited
The MOX program is
experimental in that no reactor has ever been
operated with fuel derived from weapons-grade
plutonium. European experience with MOX includes
fuel derived from irradiated nuclear fuel, a
waste product. Duke Power propose to use
something quite different: fuel made from
dismantled plutonium weapons. The fuel made from
dismantled plutonium weapons would be comprised
of a different mix of radioactive isotopes. For
example, the plutonium in MOX fuel planned for
Catawba and McGuire would be 92% Pu-239, where
European reactor MOX contains just 56% of Pu-239.
Dukes reactors would be fueled with 64%
more Plutonium-239; the most dangerous isotope
which provides the explosive power of a nuclear
weapon.
Reports on Duke
Powers McGuire and Catawba reactors
describe human and technical errors which raise
questions as to safety and reliability. Without
modifications of the plants containment
vessels, inspection schedules, and maintenance
procedures, the increased danger of reactor
embrittlement may be hidden by outwardly normal
appearance. Safety margins would be reduced if
commercial power reactors designed for uranium
fuel use plutonium fuel. In her May 17, 1999 letter to Nuclear
Regulatory Commission Chairman, the Chair of the
Advisory Committee on Reactor Safeguards said,
The U.S.
Department of Energy is proposing to dispose of
some fraction of the Nation's excess
weapons-grade plutonium by converting this
plutonium into MOX for use in commercial nuclear
power plants. There is, however, rather limited
operational or regulatory experience with the use
of MOX in the U.S. Even the experience in other
countries is not extensive.
Reactor
Embrittlement
Higher energy
neutrons from plutonium are more likely to strike
reactor parts such as the stainless steel
containment vessel. This neutron bombardment
degrades the metal parts of the reactor and the
metal becomes brittle. An embrittled reactor may
look unchanged, but it will not perform as well
under extreme conditions. For example, an event
causes the water level in the reactor to drop.
Normally, the heated water is replaced by cold
water from outside the reactor. However, this
cold water bath may cause the embrittled metal
part to fail and a minor reactor failure becomes
a major one. Embrittlement of reactor parts is a
well-known phenomenon and has caused premature
closing of commercial power reactors. The
additional neutron bombardment caused by MOX
fuels plutonium will increase the tendency
of parts to wear out and fail.
Plutonium Fuel
is Unstable
French test
results suggest that plutonium fuel is more
unstable than uranium fuel. In 1997 a MOX fuel
rod violently ruptured when subjected to test
conditions designed to simulate an accident. The
uranium fuel rod in that test did not rupture.
The May 17, 1999 Advisory Committee on Reactor
Safeguards letter to Nuclear Regulatory
Commission Chairman states,
We
are aware of experimental studies that
show there to be enhanced release of
fission gases to the fuel-cladding gap
during reactor operations with MOX
relative to conventional fuels. This may
simply be an effect caused by fuel
temperature. We are also aware of
anecdotal accounts of the results of
VERCOURS tests in France dealing with the
release of volatile radionuclides such as
cesium from MOX under severe accident
conditions. Results of these tests
revealed that during the early stages of
core degradation, releases of volatile
radionuclides from MOX are more extensive
than from conventional fuels at similar
levels of burnup.
Safety
and Reliability Problems at Catawba and McGuire
Hazards in nuclear
plants are a combination of human and technical
errors. Both types of error are noted in the
Nuclear Regulatory Commissions Plant
Performance Reviews of the McGuire, and Catawba
reactors.
The Department of
Energys Environmental Synopsis contains a
Nuclear Regulatory Commission Systematic
Assessment of Licensee Performance (SALP) for the
Catawba, McGuire, and North Anna nuclear power
stations. However, the Nuclear Regulatory
Commission suspended the SALP program in favor of
Plant Performance Reviews (PPRs).
PPRs were completed in March 1999 for these
reactors and rate all three merely
acceptable. The PPRs note
shortcomings in ice condenser maintenance and
inspection in McGuire and Catawba reactors and
corrosion of service water pipes and auxiliary
feedwater pipes (the only source of water for
steam generators when the main feedwater system
fails), and examples of poor engineering
performance at North Anna and Catawba. I include
excerpts from the Catawba PPR:
Catawba NRC Plant
Performance Review March 25, 1999:
Unit
1 experienced a forced outage of
approximately three weeks in duration due
to blocked flow channels in portions of
the ice condenser. Problems in
maintenance programs and processes
included examples of surveillance
deficiencies for ventilation systems and
ice condensers.
The
engineering performance decline was the
result of deficiencies in auxiliary
building ventilation system testing, an
overheating event of the upper surge
tank, and degraded conditions in the Unit
1 ice condenser. While the issues were
ultimately resolved properly, each had
roots in poor engineering
performance.
Catawba
and McGuire utilize ice condensers which absorb
energy and allow smaller physical containment
structures to contain accidental radioactive
releases from the reactors. Ice condensers must
work during a reactor emergency-as an air bag
must work during an auto accident. The Donald C.
Cook nuclear plant uses similar technology was
shut down because of ice condenser problems. No
nuclear plant should use MOX until these ice
condenser problems are solved.
The
NRC has a mandate to protect public
health and safety. The findings from D C
Cook indicate that both of its units may
not have protected the public had there
been an accident. The NRC does not know
about the adequacy of the other ice
condensers. The people living around
these plants should be protected by solid
designs and functioning safety equipment,
not by sheer luck. David
Lochbaum, Union of Concerned Scientists
Backgrounder on Ice Condensers, 5/26/98
Public
Health Impacts From Radiation Releases
MOX fuel has a
greater quantities of plutonium and other
hazardous radioactive isotopes such as Americium
241 and Curium 242--actinide elements which would
cause additional harmful radiation exposure to
the public during a failure of the reactor
containment structure.
Public
attention has been drawn to the higher
actinide inventories available for
release from MOX than from conventional
fuels. Significant releases of
actinides during reactor accidents would
dominate the accident consequences.
Models of actinide release now available
to the NRC staff indicate very small
releases of actinides from conventional
fuels under severe accident
conditions. (emphasis added)
~Letter from
Advisory Committee on Reactor Safeguards
to Nuclear Regulatory Commission
Chairman, May 17, 1999
The
release of these more toxic radioactive elements
would cause more fatalities immediately following
the accident, and would cause more cancers in the
years following the breach. A recent study by the
Nuclear Control Institute estimates that the risk
to the public near McGuire or Catawba of
contracting a deadly cancer following a severe
accident will increase by nearly 40% when the
plants start using plutonium fuel.
A study by Dr.
Edwin Lyman estimated the number of cancer deaths
that could result from an accident at a plant
using MOX fuel:
A reactor
using weapons-grade MOX fuel in one-third
of its core contains, on average, about
three times more plutonium 239, five
times more americium 241, and four times
more curium 242 than a reactor using only
LEU (low enriched uranium) fuel. Compared to an
LEU-fueled reactor, a severe accident at
a reactor with a one-third weapons grade
MOX core, involving a core meltdown and
containment failure or bypass, could
cause approximately 30% more cancer
fatalities, corresponding to hundreds or
even thousands of additional cancer
deaths, depending on the type of
accident.
The annual
risk of contracting a fatal cancer as a
result of a severe accident would
increase by nearly 40 percent for an
average individual living near a nuclear
plant if the plant were to load
weapons-grade MOX in one-third of its
core.
~Nuclear Control Institute
MOX Safety Report, March 1999
Dr.
Lymans study indicates that the
increase in risk associated with the use
of weapons-grade MOX in typical U.S.
power reactors is so large that,
according to NRC staff regulatory
guidance, an application for a license
amendment to use MOX would not
normally be considered. See Office
of Nuclear Energy Research, Regulatory
Guide 1.174.
~Nuclear Control Institute
Background Paper January 21, 1999
Plutonium
Fuel Transportation Hazards
Emergency response
to rail or highway accidents must be
well-prepared and rapid. Delays in response to
accidents which involve the release of
radioactive material would expose unknown numbers
of people to negative health effects. In 1996, a
DOE Transport and Safeguards Division Safe Secure
Transport (SST) trailer carrying nuclear weapons
slid off the road and rolled over in rural
Nebraska. Four hours elapsed before DOE
headquarters were notified, and it was 20 hours
before a Radiological Assistance Program team
determined there was no release. A similar delay
in response to a MOX fuel accident could make
effective emergency response dangerous and
clean-up impossible. The following comment by the
Georgia Environmental Protection Division cites
vehicular tests of powdered materials deposited
on roadways and takes issue with the DOEs
approach to emergency response to accidental
plutonium fuel releases.
After
passage of about 100 cars only a small
fraction of the original contamination
remained on the road surface. Unless
emergency officials promptly close the
accident scene to vehicle traffic (an
unlikely situation), emergency responders
may face an incident scene that is,
unknown to them, extremely hazardous due
to respirable plutonium. Post emergency
actions may also be complicated due to
the enhanced spread of contamination by
vehicle traffic. ~Georgia
Environmental Protection Division
comments on DOE SPD DEIS
Many
rural communities in South Carolina, North
Carolina, and Virginia resemble Nebraska in that
fire departments and emergency first-responders
are entirely volunteer. This does not imply a
lack of dedication, but limited resources do not
allow volunteers to be prepared for every
possible emergency. I served as a volunteer
fireman in NC for many years and our experience,
training, and equipment did not prepare us for
radionuclide transport accidents.
Complete
Information Has Not Been Made Public
Duke, Cogema,
Stone & Webster (DCS) and its subcontractors
must be subject to full public scrutiny. The
DOEs Environmental Synopsis is at least two
steps removed from the original data which the
DOE required prospective contractors to submit in
a Request For Proposal (#DE-RP02-98CH10888). Such
third-hand information does not provide a
sufficient level of detail required for a
thorough independent analysis. I hereby repeat
our request first made in June 1999 that DOE make
all information on the MOX project submitted by
DCS (Duke Engineering & Services, COGEMA
Inc., and Stone & Webster) available for
review to members of the affected public. These
data include:
DOEs
Environmental Critique DCS environmental
data and analyses for design, licensing,
construction, operation, and eventual
decontamination and decommissioning of a
MOX facility,
DCS
environmental data and analyses for
irradiation of MOX fuel in existing
domestic, commercial reactors,
DOE
projections of populations surrounding
the proposed reactor sites and
evaluations of air dispersal patterns,
Oak Ridge
National Laboratory data on the expected
radionuclide activities in MOX fuel
compared to that in low enriched uranium
fuel used in reactor accident analyses,
and
DCS
data used in computer models for determining
radiation doses from normal operations and
accident scenarios.
The NRC must
address all the problems outlined above in its
pending environmental impact statement. Please
find attached 23 pages of documents comprised of
largely reports on Dukes Catawba and
McGuire operations from 1999 to 2001.
Respectfully
submitted,
Louis Zeller
Attachments
NRC
Plant Performance Reviews
Shortcomings,
problems, errors, and poor engineering
performance
McGuire NRC
Plant Performance Review, March 25, 1999
These Duke Power
plants in North Carolina began operation in 1981
and 1983. The following excerpts are from the
NRCs PPR:
...shortcomings
in oversight of diesel generator vendors were
noted.
Several
human performance errors during routine plant
evolutions were identified...
Minor
program and procedure problems still indicate
room for improvement. In addition to core
inspections, a regional initiative inspection is
planned for ice condenser inspections during the
Unit 2 refueling...
An area for
improvement was engineering programs and
processes such as ... procedures and work
instructions for maintenance and calibration of
instrumentation....
... some
fire protection system maintenance material
conditions weaknesses have been noted...
Self-identified
problems with fire barrier penetration seals were
reported to the NRC and improvements are being
made.
Catawba NRC
Plant Performance Review, March 25, 1999
These Duke Power
reactors began operation in 1985 and 1986. The
following exerpts are from the NRCs PPR:
Unit 1
experienced a forced outage of approximately
three weeks in duration due to blocked flow
channels in portions of the ice condenser.
Engineering
performance continued to be acceptable but
declined since the last assessment as a result of
emergent issues rooted in shortcomings in
engineerings performance.
Examples of
poorly supported or non-conservative operability
or root cause determinations were noted.
Problems in
maintenance programs and processes included
examples of surveillance deficiencies for
ventilation systems and ice condensers.
The
engineering performance decline was the result of
deficiencies in auxiliary building ventilation
system testing, an overheating event of the upper
surge tank, and degraded conditions in the Unit 1
ice condenser. While the issues were ultimately
resolved properly, each had roots in poor
engineering performance.
Nuclear
Regulatory Commission
Office of Public Affairs
-- Region II
61 Forsyth Street, Suite
23T85, Atlanta, GA 30303
Ken Clark (Phone:
404/562-4416, E-mail: kmc2@nrc.gov)
Roger Hannah (Phone
404/562-4417, E-mail: rdh1@nrc.gov)
|
No:
II-98-35
May 11, 1998
NRC
OFFICIALS SEND INSPECTION TEAM TO CATAWBA
Augmented
Inspection Team Will Inspect and Assess Recent
Event
Nuclear Regulatory
Commission officials today dispatched an
Augmented Inspection Team to the two-unit Catawba
nuclear power plant, operated by Duke Energy
Company near Rock Hill, South Carolina. The team
will assess the circumstances of an event on May
7 which left the Catawba Unit 1 auxiliary
feedwater system in a condition different from
its design. NRC officials said no accident
occurred. Duke engineers told the agency the
plant suffered no adverse effects. NRC's interest
is in learning how a failure in the unit's non
safety-related, secondary condensate system
resulted in operators declaring inoperable all
trains of the safety-related auxiliary feedwater
system. Catawba has a primary and secondary water
system. The primary system cools the reactor by
circulating water directly through the core. It
then passes through thousands of tubes into a
large cylindrical tank known as a steam
generator. The steam generator is filled with
water supplied by the secondary system. This
secondary system water serves two functions: (1)
it absorbs heat from the primary reactor cooling
system, and (2) it produces steam which turns
turbines to generate electricity. After turning
the turbines, this steam is condensed back into
water and normally recirculates through the
feedwater system to produce more steam. The
auxiliary feedwater system serves as a backup to
the feedwater system. On May 7, plant operators
determined that, following a planned power
reduction, tanks which hold water for use in the
auxiliary feedwater system registered a water
temperature in excess of system design limits.
The operators declared three auxiliary feedwater
pumps inoperable due to uncertainty related to
their operation under higher water temperatures.
Duke attributed the cause to an improper setting
on a pump recirculation valve. This erroneous set
point, the company believes, resulted in a higher
than normal flow of water during the power
reduction, diverting some of the hotter water to
the auxiliary feedwater system tank. Operators
returned water temperatures to normal and
declared the auxiliary feedwater system operable.
Permanent corrective actions are being evaluated.
NRC officials said members of the inspection team
will arrive at the site Monday afternoon and
Tuesday morning. Team leader Kerry Landis, a
branch chief in the NRC Atlanta regional office's
Division of Reactor Projects, will be available
to discuss preliminary team findings with the
public and the press at the conclusion of the
inspection.
Nuclear
Regulatory Commission
Office of Public Affairs
-- Region II
61 Forsyth Street, Suite
23T85, Atlanta, GA 30303
Ken Clark (Phone:
404/562-4416, E-mail: kmc2@nrc.gov)
Roger Hannah (Phone
404/562-4417, E-mail: rdh1@nrc.gov)
|
No: II-98-47
June 12, 1998
NRC
TO MEET WITH DUKE ENERGY ON JULY 8 TO DISCUSS
NUCLEAR POWER PLANT ICE CONDENSERS
Status
of Systems at McGuire and Catawba to Be Discussed
Officials from the
Nuclear Regulatory Commission and Duke Energy Corporation
will meet in Atlanta on July 8 to discuss the
status of the ice condenser safety system at the
McGuire nuclear power plant in North Carolina and
the Catawba nuclear power plant in South
Carolina. The meeting will be held at 10:00 a.m.
(EDT) in NRC offices on the 24th floor of the
Atlanta Federal Center, located at 61 Forsyth
Street, S.W. The meeting is open to observation
by the public and media, and NRC officials will
be available at its conclusion to answer
questions from observers who attend. Ice
condensers are incorporated into some
Westinghouse pressurized water reactor
containment building designs. They are
constructed so that steam released during an
accident wil be directed through borated ice
where it is cooled and condensed. This serves to
mitigate buildup of pressure on the containment
building walls.
Nuclear
Regulatory Commission
Office of Public Affairs
-- Region II
61 Forsyth Street, Suite
23T85, Atlanta, GA 30303
Ken Clark (Phone:
404/562-4416, E-mail: kmc2@nrc.gov)
Roger Hannah (Phone
404/562-4417, E-mail: rdh1@nrc.gov)
|
No: II-99-43
July 12, 1999
NRC
STAFF SETS ENFORCEMENT CONFERENCE WITH DUKE
ENERGY
TO
DISCUSS APPARENT VIOLATIONS AT CATAWBA NUCLEAR
STATION
The Nuclear
Regulatory Commission staff has scheduled a
predecisional enforcement conference in Atlanta
on Tuesday, July 20, to discuss with Duke Energy
Corporation apparent violations of NRC
requirements related to the Unit 1 and Unit 2 ice
condensers at the Catawba Nuclear Station near
York, South Carolina. The meeting will be held at
1:00 p.m. in Bridge Conference Room D of the Sam
Nunn Atlanta Federal Center at 61 Forsyth Street.
It is open to observation by interested members
of the public and news media representatives. NRC
officials will be available at its conclusion to
answer questions from interested observers.
NRC officials said
the apparent violations include the potential
inoperability of the Unit 2 ice condenser doors
due to ice buildup, the failure to promptly
identify and correct ice condenser blockage and
damaged ice containers in both units, the failure
to perform adequate inspections for foreign
debris in the ice condensers, and the failure to
properly install ice condenser components as
designed.
Ice condensers are
incorporated into some Westinghouse pressurized
water reactor containment building designs. They
are constructed so that steam released during an
accident will be directed through borated ice
where it is cooled and condensed. This serves to
mitigate buildup of pressure on the containment
building walls.
The decision to
hold a predecisional enforcement conference does
not mean that a determination has been made that
violations have occurred or that enforcement
action will be taken. The purpose is to discuss
the apparent violations, their causes and safety
significance; to provide the licensee with an
opportunity to point out errors that may have
been made in NRC inspection reports; and to
enable the licensee to outline its proposed
corrective actions.
No decision on the
apparent violations or any contemplated
enforcement action, such as a civil penalty, will
be made at the conference. Those decisions will
be made by NRC officials at a later time.
Nuclear
Regulatory Commission
Office of Public Affairs
-- Region II
61 Forsyth Street, Suite
23T85, Atlanta, GA 30303
Ken Clark (Phone:
404/562-4416, E-mail: kmc2@nrc.gov)
Roger Hannah (Phone:
404/562-4417, E-mail: rdh1@nrc.gov)
|
No:
II-97-70
September 23, 1997
>NRC
STAFF TO HOLD CONFERENCE WITH DUKE POWER COMPANY
TO
DISCUSS
APPARENT VIOLATIONS AT McGUIRE NUCLEAR PLANT
The Nuclear
Regulatory Commission staff will hold a
predecisional enforcement conference with Duke
Power Company on Wednesday, October 1, to discuss
apparent violations of NRC regulations involving
ice condenser doors at the McGuire nuclear power
plant near Huntersville, North Carolina.
The apparent
violations involve the company's failure to
ensure that ice condenser inlet doors on Unit 2
would be able to open if needed and a failure to
perform adequate corrective actions based on
industry experience and operational events at
McGuire.
The ice condenser
is a passive accident mitigation system
containing about two and one-half million pounds
of borated ice. If an accident were to occur, the
ice condenser system would condense steam and
lower pressure in the plant's containment
structure. The ice is located behind a number of
doors designed to open when the pressure in
containment reaches a certain level above the
pressure inside in the ice condenser area.
In July, McGuire
plant employees determined that 10 of the 48 ice
condenser inlet doors in lower containment were
incapable of opening with less force than
specified in the plant's technical specifications
and may not have opened in an accident situation.
The meeting will
be held in the NRC Atlanta office, located at 61
Forsyth Street, Room 24T20, at 10:00 a. m. It
will be open to observation by the public.
NRC officials said
the decision to hold a predecisional enforcement
conference does not mean that a determination has
been made that a violation has occurred or that
enforcement action will be taken.
The purpose is to
discuss apparent violations, their causes, and
safety significance; to provide the licensee with
an opportunity to point out any errors that may
have been made in NRC inspection reports; and to
enable the company to outline its proposed
corrective actions.
No decision on the
apparent violations or any contemplated
enforcement action, such as a civil penalty, will
be made at the conference. Those decisions will
be made by NRC officials at a later time.
Nuclear
Regulatory Commission
Office of Public Affairs
Washington DC 20555
Telephone: 301/415-8200
-- E-mail: opa@nrc.gov
|
No. 99-219
October 15, 1999
NRC
TO ALLOW DUKE ENERGY TO SUBMIT
EARLY
LICENSE RENEWAL APPLICATIONS
The Nuclear
Regulatory Commission has granted a request from
the Duke Energy Corporation toallow the company
to submit applications to renew the licenses for
its McGuire Unit 2 and the two Catawba nuclear
power plants earlier than usually permitted.
NRC regulations
specify that license renewal applications may not
be submitted to the Commission earlier than 20
years before the expiration of the current
40-year operating license. This limit is designed
to ensure that sufficient operating experience is
accumulated to identify any plant-specific aging
concerns. However, in amending this license
renewal rule in 1995, the Commission indicated it
would consider an exemption to this requirement
if sufficient information was available on a
plant-specific basis to justify it.
By June 2001, the
earliest date the NRC said it will accept a
license renewal application from Duke, McGuire
Unit 1 will have achieved the required 20 years
of operation; Unit 2 will have 18.3 years;
Catawba Unit 1 will have 16.5 years and 15.3
years for Unit 2. In a safety evaluation, the NRC
determined that the operating experience of
McGuire Unit 1, in conjunction with the
substantial number of years for the other three
units, should be sufficient to identify any aging
concerns applicable to all four units.
McGuire, 17 miles
south of Charlotte, N.C., and Catawba, six miles
northwest of Rock Hill, S.C., are two-unit
stations utilizing pressurized water reactors
with ice-condenser containments having a rated
power output of about 1130 megawatts each. The
four plants are sufficiently similar in design,
operation and maintenance that the operating
experience of McGuire Unit 1 should apply to the
other three units, according to the NRC staff.
In its request for
early license renewal, Duke Energy explained that
regular and systematic exchanges of information
among its nuclear stations provide a means to
continually improve plant programs. Duke Energy
plans to submit license renewal requests for all
four units simultaneously, to expedite processing
and reduce costs.
The current
operating license for McGuire Unit 1 expires in
2021, and for McGuire Unit 2, in 2023. The
current operating license for Catawba Unit 1
expires in 2024, and for Unit 2, in 2026.
Once submitted,
the license renewal applications will have to
meet the same requirements NRC is using in
evaluating other license renewal applications. If
granted, the renewed licenses will have the
effect of extending the operating life of each
plant by as many as 20 years.
The exemption was
published in the Federal Register
October 8.
Nuclear
Regulatory Commission
Office of Public Affairs
-- Region II
61 Forsyth Street, Suite
23T85, Atlanta, GA 30303
Ken Clark (Phone:
404/562-4416, E-mail: kmc2@nrc.gov)
Roger Hannah (Phone
404/562-4417, E-mail: rdh1@nrc.gov)
|
No: II-99-26
April 5, 1999
NRC
FINDS PERFORMANCE 'ACCEPTABLE'
AT
MCGUIRE IN LATEST REVIEW
The Nuclear
Regulatory Commission staff has found that safety
performance remains acceptable in the NRC's
latest plant performance review at the McGuire
nuclear power plant, operated by Duke Power
Company near Huntersville, North Carolina.
Charlotte In a letter to Duke Power which
outlined the results of the review, which ran
from March 1997 through January 1999, Charles R.
Ogle, an official in the agency's Atlanta
regional office, said "overall performance
at McGuire was acceptable" and that
"strong management involvement resulted in
improvements" in the area of plant
operations. He said performance also improved in
maintenance and plant support and that
engineering performance was
"consistent."
Ogle said that the
NRC plans to conduct inspections from the Atlanta
regional office on the plant's ice condensers,
fire protection system, and development of an
Independent Spent Fuel (Dry Cask) Storage
Installation, in addition to its normal
inspection program, during the next assessment
period at McGuire
The text of the
plant performance review letter is available from
the NRC Region II Office of Public Affairs and on
the NRC web site at: http://www.nrc.gov/OPA/ppr.
NRC reviews safety
performance twice a year at every licensed
nuclear power plant in the nation. These reviews
give the agency staff an integrated assessment of
plant performance and provide a basis for
planning inspection activities.
Plant performance
reviews are being used by the NRC as an interim
measure to monitor nuclear power plant safety.
The agency began using it for this purpose after
suspending the Systematic Assessment of License
Performance (SALP) process until a new assessment
program is developed. Previously, SALP reports
were issued every 12 to 24 months.
The new reactor
oversight and assessment program being developed
will provide quarterly performance reports, based
on a number of performance indicators and on
inspection findings. This program will be tested
at eight sites beginning in June and will be
extended to all plants next January.
NRC
Performance Summaries
Catawba
1
Initiating
Events
Significance:
TBD Feb 16, 2001
Identified By: NRC
Item Type: AV Apparent Violation
Failure to Promptly Identify and Correct the
Unit 1 Residual Heat Removal System Water Hammer
Condition
An apparent violation of 10 CFR 50, Appendix B,
Criterion XVI was identified for the failure to
identify a root cause and establish effective
corrective actions to prevent repetitive water
hammer events in the Unit 1 residual heat removal
(ND) system which have caused the repeated
failure of snubbers on supports 1-R-ND-0226 and
1-R-ND-0596. (Section 40A2.b.(2).2)
Inspection Report# : 2001003
Mitigating
Systems
Significance: G
Mar 30 2001
Identified By: NRC
Item Type: FIN Finding
Failed to Demonstrate Performance of the
Station Drinking Water System as Backup Cooling
Water to the Unit 1 and 2 A Train Charging Pumps
The licensee failed to demonstrate that the
performance or condition of the station drinking
water system, a risk-important system that
provides backup cooling water to the Unit 1 and 2
A train charging pump motors and bearing oil
coolers, was being effectively controlled through
the performance of appropriate preventive
maintenance (including surveillance activities).
This resulted in a failure to recognize and
correct a degraded system pressure condition,
until it was identified by the inspectors. The
degraded pressure condition was determined to be
of very low safety significance because an
analysis performed by the licensee demonstrated
that the backup function to cool the charging
pumps and motors would have been provided at the
degraded pressure (Section 1R12.2).
Inspection Report# : 2000006
Significance: G
Mar 30, 2001
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Adequately Perform TS SR 3.4.9.3
for Pressurizer Heaters
A non-cited violation was identified regarding
the licensees failure to properly perform
Technical Specification Surveillance Requirement
3.4.9.3, which verifies that pressurizer heaters
can be automatically transferred from their
normal power supplies to their emergency power
supplies. Once identified, the portion of the
automatic circuit that had been omitted from the
test was properly tested on February 5, 2001, and
was verified to be functional. This finding had a
credible impact on safety because the licensee
had never demonstrated the full automatic
capability of the power supply transfer circuitry
for the pressurizer heaters, which are important
for maintaining pressurizer pressure control
during a loss of offsite power event. The finding
was also the latest in a number of missed
surveillance requirements identified at Catawba
over the last two to three years. This finding
was of very low safety significance because the
circuit was functional when tested and because of
provisions in the licensee's emergency procedures
for manually aligning the heaters to their
emergency power source had the automatic transfer
failed during a loss of normal power event
(Section 1R22).
Inspection Report# : 2000006
Significance: G
Feb 16, 2001
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Identify Conditions Adverse to
Quality - two examples
The first example of a non-cited violation of 10
CFR 50, Appendix B, Criterion XVI was identified
for a failure to identify a condition adverse to
quality which contributed to a Unit 1 reactor
vessel level instrument system (RVLIS) channel
being inoperable. A quality control inspector did
not initiate a Problem Investigation Process
report after identifying that a RVLIS system
terminal board was not reconnected (wired) in
accordance with electrical drawings. Because of
an electrical drawing error, the terminal board
was then wired incorrectly and resulted in a
failure to meet Technical Specification 3.3.3.
Function 4 requirements for an inoperable RVLIS
channel from June 1999 to November 4, 2000.
Because other indications would have been
available to the operators to mitigate the
consequences of an accident, and based on the
probability that the operators would have used
the conservative indication of decreasing reactor
vessel level from the operable RVLIS channel, the
inspectors determined that this issue was of very
low safety significance. (Section 40A2.a.(2).2)
The second example of a non-cited violation of 10
CFR 50, Appendix B, Criterion XVI was identified
for a failure to identify a condition adverse to
quality which contributed to not recognizing that
four post accident monitoring control room
recorders in Unit 1 were inoperable from
September 24 through September 29, 2000, and
degraded from September 29 through October 19,
2000. Specifically, operators did not review
applicable electrical drawings in order to
identify which components were supplied from a
failed electrical breaker. Consequently, they did
not recognize that post accident monitoring
control room recorders, which are used in the
emergency operating procedures to determine
mitigation strategies, were no longer operable.
Because other indications would have been
available to the operators to use in lieu of
these accident monitoring recorders and because
the Technical Specification Limiting Condition
for Operation requirements were not exceeded, the
inspectors determined that this issue was of very
low safety significance. (Section 40A2.a.(2).3)
Inspection Report# : 2001003
Significance:G Feb
16, 2001
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Meet 10 CFR 50, Appendix B,
Criterion III and XI for Unit 1 RIVLIS
10 CFR 50, Appendix B, Criterion III, requires in
part that the design bases is correctly
translated into drawings. 10 CFR 50, Appendix B,
Criterion XI, requires in part that all testing
required to demonstrate that components will
perform satisfactorily in service is identified
and performed. To the contrary, an error in the
electrical drawings for the Unit 1 reactor vessel
level indication system (RVLIS) circuitry was
introduced during a previous drawing revision on
July 1, 1985, which led to the improper wiring of
the RVLIS instrumentation in a June 1999
modification. Following the modification
activities, the licensee did not develop an
adequate post modification testing plan for the
RVLIS electrical circuitry, resulting in one
channel of RVLIS being inoperable for 18 months.
This finding was determined to have very low
safety significnace and is captured in the
licensee's corrective action program under PIP
C-00-05558 (Section 4OA7).
Inspection Report# : 2001003
Significance: G
Jun 24, 2000
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Scope an Accident Mitigating
Function Associated with ECCS Leak Detection in
the Maintenance Rule
The licensee failed to include in its maintenance
rule scope an accident mitigating function for a
control room alarm associated with emergency core
cooling system post-accident leak detection
capability. The alarm was tied to residual heat
removal and containment spray pump room sump
levels and was identified in 1998 as a mitigating
function, as described in the Catawba Updated
Final Safety Analysis Report. As a result, two
functional failures were not properly classified
in February 2000. This issue was characterized as
a non-cited violation of 10 CFR 50.65 (b)(2) and
was determined to have very low safety
significance because the licensee's scoping and
functional failure determination errors did not
directly result in additional unavailability of
the alarm function (Section 1R12.2).
Inspection Report# : 2000003
Significance: G
Jun 24, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Provide Adequate Procedures for
Performing Maintenance on Safety-Related Sump
Pump Level Switches
Residual heat removal and containment spray pump
room sump level alarm function was lost for
several months up to February 2000 due to
inadequate maintenance procedures associated with
sump level switch calibrations. This issue was
characterized as a non-cited violation of
Technical Specification 5.4.1 and was determined
to be of very low safety significance due to the
availability of other emergency core cooling
system leak detection methods (Section 4OA3.2).
Inspection Report# : 2000003
Occupational
Radiation Safety
Significance: G
Sep 23, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Implement Radiation Control
Procedures for Posting Extra High Radiation Areas
as Required by TS 5.4.1.a
A single event, resulting in two non-cited
violations, involved: (1) a failure to implement
radiation control procedures for posting an extra
high radiation area as required by TS 5.4.1.a.;
and (2) failure to lock or control entrance to an
extra high radiation area as required by
Technical Specification 5.7.2 and Title 10 CFR
Part 20.1601. This event was determined to be of
very low safety significance because minimal
radiation exposure was received by the workers
and inadvertent entry into the area of concern
(i.e., containment building in the area near the
personnel air lock) would not immediately result
in workers being in radiation fields greater than
1000 milliroentgen equivalent man per hour
(Section 2OS1).
Inspection Report# : 2000004
Significance: G
Sep 23, 2000
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Control Access to High Radiation
Areas as Required by 10 CFR Part 20.1601 and TS
5.7.2
A single event, resulting in two non-cited
violations, involved: (1) a failure to implement
radiation control procedures for posting an extra
high radiation area as required by TS 5.4.1.a.;
and (2) failure to lock or control entrance to an
extra high radiation area as required by
Technical Specification 5.7.2 and Title 10 CFR
Part 20.1601. This event was determined to be of
very low safety significance because minimal
radiation exposure was received by the workers
and inadvertent entry into the area of concern
(i.e., containment building in the area near the
personnel air lock) would not immediately result
in workers being in radiation fields greater than
1000 milliroentgen equivalent man per hour
(Section 2OS1).
Inspection Report# : 2000004
Significance: G
Jun 24, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Prevent the Release of Radioactive
Byproduct Material from the Radiological Control
Area and Plant Site
A non-cited violation was identified for the
failure to comply with the requirements of 10 CFR
20.1802. Specifically, on April 7, 2000, the
licensee failed to prevent the release of
radioactive byproduct material (e.g., a
radioactive particle on a contract employee's
lanyard) from the radiological control area and
plant site. Based on the activity of the particle
and the resulting occupational dose assessment
for the affected contract employee, this finding
was determined to be of very low significance
(Sections OS2, 2PS3).
Inspection Report# : 2000003
Physical
Protection
Significance: G
Jun 24, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Secure Two Vital Area Openings
Exceeding 96 Square Inches in February 1999
A non-cited violation of the Physical Security
Plan was identified for the licensee's failure to
secure two vital area openings exceeding 96
square inches in February 1999. This issue was
determined to have very little significance,
given the non-predictable basis of the failures
and the fact that there was no evidence that the
vulnerabilities had been exploited (Section
3PP2).
Inspection Report# : 2000003
Miscellaneous
Significance:
N/A Feb 16, 2001
Identified By: NRC
Item Type: FIN Finding
Identification and Resolution of Problems
Overall, the licensee's corrective action program
was effective at identifying, evaluating, and
correcting problems. The threshold for entering
problems into the corrective action program was
sufficiently low. Reviews of operating experience
information were comprehensive. In general, the
licensee properly prioritized items (by Action
Category) in its corrective action program
database, which ensured that timely resolution
and appropriate causal factor analyses were
employed commensurate with safety significance.
Some exceptions were noted in the area of problem
identification, where all relevant issues of
problems were not identified and equipment
performance was adversely affected. The
inspection identified three exceptions in the
area of prioritization and evaluation of issues,
where more comprehensive root cause
determinations would have provided more effective
evaluations and corrective actions. In the area
of effectiveness of corrective actions, it was
noted that the corrective action program was not
timely in resolving various documentation
deficiencies with Technical Specification (TS)
surveillances, Updated Final Safety Analysis
Report changes and TS bases changes. Previous
non-compliance issues documented as non-cited
violations were properly tracked and resolved via
the corrective action program. The results of the
last comprehensive corrective action program
audit conducted by the licensee (September 1999)
were properly entered and dispositioned in the
corrective action program. Based on discussions
with plant personnel and the apparently low
threshold for items entered in the corrective
action program database, the inspectors concluded
that workers at the site generally felt free to
raise safety concerns to their management.
Inspection Report# : 2001003
Significance:
N/A Dec 23, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Technical Specification 5.4.1 and Regulatory
Guide 1.33, Section 7, for failing to have
adequate procedures to control the release of
radioactive material during a pressurizer gas
space venting evolut
Technical Specification 5.4.1 and Regulatory
Guide 1.33, Section 7, for failing to have
adequate procedures to control the release of
radioactive material during a pressurizer gas
space venting evolution on October 14, 2000, as
described in the licensee's corrective action
program. Reference PIPs C-00-04914 and 05241.
Inspection Report# : 2000005
Last modified :
May 03, 2001
Catawba
2
Initiating
Events
Significance: G
Sep 23, 2000
Identified By: Licensee
Item Type: FIN Finding
Reactor Trip Caused by Moisture Intrusion into
Main Feedwater Pump 2B Speed Control Circuitry
Poor workmanship and inadequate oversight of
turbine building roof repairs, coupled with
inadequately constructed roof drainage systems,
resulted in a June 5, 2000, Unit 2 reactor trip.
Water from heavy rains that day could not be
properly drained from the turbine building roof,
partially due to debris and other roofing
material that had collected in the drainage
system. Water overflowed from the roof and into
the turbine building, and leaked into the 2B main
feedwater pump turbine speed control cabinet. A
secondary plant transient resulted, which
ultimately led to a turbine trip/reactor trip.
This issue was determined to be of very low
safety significance because it did not affect the
ability of mitigating systems to perform their
safety functions (Section 4OA3.1).
Inspection Report# : 2000004
Mitigating
Systems
Significance: GMar
30, 2001
Identified By: NRC
Item Type: FIN Finding
Failed to Demonstrate Performance of the
Station Drinking Water System as Backup Cooling
Water to the Unit 1 and 2 A Train Charging Pumps
The licensee failed to demonstrate that the
performance or condition of the station drinking
water system, a risk-important system that
provides backup cooling water to the Unit 1 and 2
A train charging pump motors and bearing oil
coolers, was being effectively controlled through
the performance of appropriate preventive
maintenance (including surveillance activities).
This resulted in a failure to recognize and
correct a degraded system pressure condition,
until it was identified by the inspectors. The
degraded pressure condition was determined to be
of very low safety significance because an
analysis performed by the licensee demonstrated
that the backup function to cool the charging
pumps and motors would have been provided at the
degraded pressure (Section 1R12.2).
Inspection Report# : 2000006
Significance:
N/A Mar 30, 2001
Identified By: NRC
Item Type: FIN Finding
Failure to Identify Two Maintenance
Preventable Functional Failures Affecting the
Unit 2 Auxiliary Feedwater System
The inspectors identified a failure to identify
two maintenance preventable functional failures
(MPFFs) affecting the Unit 2 auxiliary feedwater
system, one involving the turbine-driven
auxiliary feedwater pump, the other involving the
A motor-driven pump. Both of these occurred on
October 5, 2000, following an inadvertent
transfer of pump control to a local control
panel. Although the finding did not involve a
violation of the maintenance rule, it represented
a recurring performance problem in this area as
the latest of several missed maintenance
preventable functional failure determinations
involving different safety systems over the last
year and a half. This finding was of very low
safety significance because the failure to
identify these MPFFs did not directly affect the
ability of the auxiliary feedwater system to
perform its safety function (Section 1R12.1).
Inspection Report# : 2000006
Significance: G
Mar 30, 2001
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Adequately Perform TS SR 3.4.9.3
for Pressurizer Heaters
A non-cited violation was identified regarding
the licensees failure to properly perform
Technical Specification Surveillance Requirement
3.4.9.3, which verifies that pressurizer heaters
can be automatically transferred from their
normal power supplies to their emergency power
supplies. Once identified, the portion of the
automatic circuit that had been omitted from the
test was properly tested on February 5, 2001, and
was verified to be functional. This finding had a
credible impact on safety because the licensee
had never demonstrated the full automatic
capability of the power supply transfer circuitry
for the pressurizer heaters, which are important
for maintaining pressurizer pressure control
during a loss of offsite power event. The finding
was also the latest in a number of missed
surveillance requirements identified at Catawba
over the last two to three years. This finding
was of very low safety significance because the
circuit was functional when tested and because of
provisions in the licensee's emergency procedures
for manually aligning the heaters to their
emergency power source had the automatic transfer
failed during a loss of normal power event
(Section 1R22).
Inspection Report# : 2000006
Significance: G
Jun 24, 2000
Identified By: Licensee
Item Type: FIN Finding
Steam generator power operated relief valve
2SV-19 failed to open on April 15, 2000, due to
mispostioned nitrogen pressure regulators
Steam generator power operated relief valve
2SV-19 failed to open on April 15, 2000, due to
mispostioned nitrogen pressure regulators, which
are required to function during a design basis
event involving the loss of normally available
instrument air. The licensee determined the
mispositioned regulators to be a human
performance issue, but were not able to pinpoint
when the actual mispositioning took place. This
issue was determined to have very low safety
significance due to the availability of other
steam generator power operated relief valves and
diverse means of cooling the secondary plant
(Section 1R22.2).
Inspection Report# : 2000003
Significance: G
Jun 24, 2000
Identified By: NRC
Item Type: FIN Finding
Failure to properly classify a maintenace rule
functional failure of the Unit 2 A steam
generator power operated relief valve (2SV-19)
The licensee failed to properly classify a
maintenace rule functional failure of the Unit 2
A steam generator power operated relief valve
(2SV-19) when it failed to open on April 15,
2000. The licensee incorrectly assumed that the
valve's failure was not a functional failure
because other redundant valves were available at
the time. This issue was determined to have very
low safety significance because the licensee's
error did not result in additional equipment
unavailability (Section 1R12.1).
Inspection Report# : 2000003
Significance: G
Jun 24, 2000
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Scope an Accident Mitigating
Function Associated with ECCS Leak Detection in
the Maintenance Rule
The licensee failed to include in its maintenance
rule scope an accident mitigating function for a
control room alarm associated with emergency core
cooling system post-accident leak detection
capability. The alarm was tied to residual heat
removal and containment spray pump room sump
levels and was identified in 1998 as a mitigating
function, as described in the Catawba Updated
Final Safety Analysis Report. As a result, two
functional failures were not properly classified
in February 2000. This issue was characterized as
a non-cited violation of 10 CFR 50.65 (b)(2) and
was determined to have very low safety
significance because the licensee's scoping and
functional failure determination errors did not
directly result in additional unavailability of
the alarm function (Section 1R12.2).
Inspection Report# : 2000003
Significance: GJun
24, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Provide Adequate Procedures for
Performing Maintenance on Safety-Related Sump
Pump Level Switches
Residual heat removal and containment spray pump
room sump level alarm function was lost for
several months up to February 2000 due to
inadequate maintenance procedures associated with
sump level switch calibrations. This issue was
characterized as a non-cited violation of
Technical Specification 5.4.1 and was determined
to be of very low safety significance due to the
availability of other emergency core cooling
system leak detection methods (Section 4OA3.2).
Inspection Report# : 2000003
Barrier
Integrity
Significance: G
Jun 24, 2000
Identified By: NRC
Item Type: FIN Finding
Failure to properly evaluate plant risk
associated with emergent work for the Unit 2
hydrogen ignition system on April 27, 2000.
The licensee did not properly evaluate plant risk
associated with emergent work for the Unit 2
hydrogen ignition system on April 27, 2000. As a
result, the unit was in an unevaluated increased
risk condition while planned work associated with
the containment spray system was ongoing. This
condition was allowed by Technical Specifications
and plant procedures, but plant procedures
required that a written contingency plan be
developed prior to the work commencing, which was
not done. This issue was of very low safety
significance due to the availability of diverse
and redundant systems designed to accomplish the
hydrogen mitigation and containment pressure
control functions (Section 1R13).
Inspection Report# : 2000003
Occupational
Radiation Safety
Significance: G
Jun 24, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Prevent the Release of Radioactive
Byproduct Material from the Radiological Control
Area and Plant Site
A non-cited violation was identified for the
failure to comply with the requirements of 10 CFR
20.1802. Specifically, on April 7, 2000, the
licensee failed to prevent the release of
radioactive byproduct material (e.g., a
radioactive particle on a contract employee's
lanyard) from the radiological control area and
plant site. Based on the activity of the particle
and the resulting occupational dose assessment
for the affected contract employee, this finding
was determined to be of very low significance
(Sections OS2, 2PS3).
Inspection Report# : 2000003
Physical
Protection
Significance: G
Jun 24, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Secure Two Vital Area Openings
Exceeding 96 Square Inches in February 1999
A non-cited violation of the Physical Security
Plan was identified for the licensee's failure to
secure two vital area openings exceeding 96
square inches in February 1999. This issue was
determined to have very little significance,
given the non-predictable basis of the failures
and the fact that there was no evidence that the
vulnerabilities had been exploited (Section
3PP2).
Inspection Report# : 2000003
Miscellaneous
Significance:
N/A Feb 16, 2001
Identified By: NRC
Item Type: FIN Finding
Identification and Resolution of Problems
Overall, the licensee's corrective action program
was effective at identifying, evaluating, and
correcting problems. The threshold for entering
problems into the corrective action program was
sufficiently low. Reviews of operating experience
information were comprehensive. In general, the
licensee properly prioritized items (by Action
Category) in its corrective action program
database, which ensured that timely resolution
and appropriate causal factor analyses were
employed commensurate with safety significance.
Some exceptions were noted in the area of problem
identification, where all relevant issues of
problems were not identified and equipment
performance was adversely affected. The
inspection identified three exceptions in the
area of prioritization and evaluation of issues,
where more comprehensive root cause
determinations would have provided more effective
evaluations and corrective actions. In the area
of effectiveness of corrective actions, it was
noted that the corrective action program was not
timely in resolving various documentation
deficiencies with Technical Specification (TS)
surveillances, Updated Final Safety Analysis
Report changes and TS bases changes. Previous
non-compliance issues documented as non-cited
violations were properly tracked and resolved via
the corrective action program. The results of the
last comprehensive corrective action program
audit conducted by the licensee (September 1999)
were properly entered and dispositioned in the
corrective action program. Based on discussions
with plant personnel and the apparently low
threshold for items entered in the corrective
action program database, the inspectors concluded
that workers at the site generally felt free to
raise safety concerns to their management.
Inspection Report# : 2001003
Significance:
N/A Dec 23, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Technical Specification 5.4.1 and Regulatory
Guide 1.33, Section 7, for failing to have
adequate procedures to control the release of
radioactive material during a pressurizer gas
space venting evolut
Technical Specification 5.4.1 and Regulatory
Guide 1.33, Section 7, for failing to have
adequate procedures to control the release of
radioactive material during a pressurizer gas
space venting evolution on October 14, 2000, as
described in the licensee's corrective action
program. Reference PIPs C-00-04914 and 05241.
Inspection Report# : 2000005
Last modified :
May 03, 2001
McGuire
1
Initiating
Events
Significance: G
Mar 17, 2001
Identified By: Licensee
Item Type: NCV NonCited Violation
Inadequate Corrective Actions for Recurring
Problems with Shutdown Operations Involving Loss
of Letdown and/or Inadvertent Reactor Coolant
System Cooldown Transients
Inadequate corrective actions (10CFR50, Appendix
B, Criterion XVI) for recurring problems with
shutdown operations involving loss of letdown
and/or inadvertent reactor coolant (NC) system
cooldown transients. During a Unit 1 shutdown
from Mode 2 to Mode 3 on March 9, 2001, NC system
temperature went below minimum temperature for
criticality due to overfeed of steam generators.
This event occurred because of ineffective
corrective actions to address procedural
deficiencies and/or equipment problems
complicating plant cooldown. This is captured in
the licensee's corrective action program under
PIP M-01-0986. This finding was determined to
have very low safety significance and is being
treated as a Non Cited Violation (Section 4OA7).
Inspection Report# : 2000007
Mitigating
Systems
Significance: G
Dec 15, 2000
Identified By: NRC
Item Type: FIN Finding
Depth and effectiveness of the licensee's
evaluation and corrective actions for failures of
the standby shutdown facility (SSF) diesel
generator.
A finding was identified associated with the
depth and effectiveness of the licensee's
evaluation and corrective actions for failures of
the standby shutdown facility (SSF) diesel
generator. The licensee's corrective actions for
recent SSF-related problems have not been
commensurate with the risk significance of the
system. A recent Problem Investigation Process
report, which documented a jacket water coolant
leak and subsequent emptying of the engine's
radiator, was not screened to include a root
cause evaluation. The licensee did not perform
comprehensive corrective actions to evaluate the
need for performing additional preventive
maintenance on the SSF diesel generator
components. The inspectors identified
vendor-recommended maintenance practices that
were not being implemented and service bulletins
authored by the vendor that were not included in
the associated controlled vendor manual located
on site. This issue was determined to have very
low safety significance because it was not
directly linked to any specific period of
unavailability for the SSF diesel generator. This
instance of ineffective corrective action was an
isolated example and is not considered indicative
of the licensee's overall corrective action
program. (Section 4OA2b).
Inspection Report# : 2000010
Significance: G
Jun 17, 2000
Identified By: Self Disclosing
Item Type: NCV NonCited Violation
Failure to Follow Emergency Procedure
Concerning Auxiliary Feedwater Suction Supplies
A non-cited violation of Technical Specification
5.4.1.a was identified for two examples of the
licensee's failure to follow the emergency
procedure generic enclosure used for maintaining
auxiliary feedwater (CA) suction sources during
reactor trip recovery. This resulted in the
inadvertent isolation of the preferred CA suction
supply and actuation of the service water system
to provide CA to the steam generators. A lack of
training and familiarity with the applicable
emergency procedure generic enclosure was found
to be a contributor to this finding. The safety
significance of this violation was very low
because the CA system was able to perform its
function of steam generator decay heat removal
(Section 04.03).
Inspection Report# : 2000008
Physical
Protection
Significance: G
Sep 16, 2000
Identified By: NRC
Item Type: NCV NonCited Violation
Failure of the Electronic Switching to Provide
the Central Alarm Station Operator with the
Capability to Properly Assess Potential
Penetrations at the Perimeter Prior to
Individuals Gaining Access
A non-cited violation of the Physical Security
Plan was identified for the failure of the
licensee's electronic switching on September 12,
2000, to provide the central alarm station
operator with the capability to properly assess
potential penetrations at the perimeter prior to
individuals gaining access to the protected area
(Section 3PP3.2)
Inspection Report# : 2000005
Miscellaneous
Significance:
N/A Dec 15, 2000
Identified By: NRC
Item Type: FIN Finding
Identification and Resolution of Problems
Overall, the licensee's corrective action program
was effective at identifying, evaluating, and
correcting problems. The threshold for entering
problems into the corrective action program was
sufficiently low. Reviews of operating experience
information were comprehensive. In general, the
licensee properly prioritized items (by Action
Category) in its corrective action program
database, which ensured that timely resolution
and appropriate causal factor analyses were
employed commensurate with safety significance.
One exception involved a recent condition adverse
to quality in which the standby shutdown
facility's (SSF) diesel generator was unavailable
following the complete draining of radiator
coolant because of heater shell pin-hole leaks.
The licensee did not perform an in-depth root
cause analysis and thorough corrective actions
following its discovery of the degraded
condition. Also, for potential safety equipment
operability issues, the licensee did not always
conduct or document thorough evaluations of
present or past inoperability. Previous
non-compliance issues documented as non-cited
violations were properly tracked and resolved via
the corrective action program. The results of the
last comprehensive corrective action program
audit conducted by the licensee (September 1999)
were properly entered and dispositioned in the
corrective action program. Based on discussions
with plant personnel and the apparently low
threshold for items entered in the corrective
action program database, the inspectors concluded
that workers at the site generally felt free to
raise safety concerns to their management.
Inspection Report# : 2000010
Last modified :
May 03, 2001
McGuire
2
Mitigating
Systems
Significance: G
Mar 17, 2001
Identified By: Licensee
Item Type: NCV NonCited Violation
Failure to Follow Procedure PT/2/A/4350/026C,
Auxiliary Shutdown Panel Verification
Failure to follow procedure (Technical
Specification 5.4.1) for PT/2/A/4350/026C,
Auxiliary Shutdown Panel Verification. The
procedure indicates that all manipulations of
controls at the panel shall be performed by a
licensed reactor operator. A non-licensed
operator performed the auxiliary shutdown
manipulations during the performance of the test,
contrary to the requirements of the procedure.
This is captured in the licensee's corrective
action program under PIP M-00-4140. This finding
was determined to have very low safety
significance and is being treated as a Non Cited
Violation (Section 4OA7).
Inspection Report# : 2000007
Significance: G
Dec 16, 2000
Identified By: Licensee
Item Type: NCV NonCited Violation
Inadequate procedure for removal of 120VAC
inverters from service
Inadequate procedure (TS 5.4.1) for removal of
Unit 2 120VAC vital inverters from service.
During plant solid RCS operation in Mode 5,
de-energizing the vital inverters resulted in an
inoperable Low Temperature Overpressure
Protection (LTOP) system required by Technical
Specification 3.4.12. The finding was determined
to have very low safety significance (Section
4OA7).
Inspection Report# : 2000006
Significance: G
Dec 15, 2000
Identified By: NRC
Item Type: FIN Finding
Depth and effectiveness of the licensee's
evaluation and corrective actions for failures of
the standby shutdown facility (SSF) diesel
generator.
A finding was identified associated with the
depth and effectiveness of the licensee's
evaluation and corrective actions for failures of
the standby shutdown facility (SSF) diesel
generator. The licensee's corrective actions for
recent SSF-related problems have not been
commensurate with the risk significance of the
system. A recent Problem Investigation Process
report, which documented a jacket water coolant
leak and subsequent emptying of the engine's
radiator, was not screened to include a root
cause evaluation. The licensee did not perform
comprehensive corrective actions to evaluate the
need for performing additional preventive
maintenance on the SSF diesel generator
components. The inspectors identified
vendor-recommended maintenance practices that
were not being implemented and service bulletins
authored by the vendor that were not included in
the associated controlled vendor manual located
on site. This issue was determined to have very
low safety significance because it was not
directly linked to any specific period of
unavailability for the SSF diesel generator. This
instance of ineffective corrective action was an
isolated example and is not considered indicative
of the licensee's overall corrective action
program. (Section 4OA2b).
Inspection Report# : 2000010
Physical
Protection
Significance: G
Sep 16, 2000
Identified By: NRC
Item Type: NCV NonCited Violation
Failure of the Electronic Switching to Provide
the Central Alarm Station Operator with the
Capability to Properly Assess Potential
Penetrations at the Perimeter Prior to
Individuals Gaining Access
A non-cited violation of the Physical Security
Plan was identified for the failure of the
licensee's electronic switching on September 12,
2000, to provide the central alarm station
operator with the capability to properly assess
potential penetrations at the perimeter prior to
individuals gaining access to the protected area
(Section 3PP3.2)
Inspection Report# : 2000005
Miscellaneous
Significance:
N/A Dec 15, 2000
Identified By: NRC
Item Type: FIN Finding
Identification and Resolution of Problems
Overall, the licensee's corrective action program
was effective at identifying, evaluating, and
correcting problems. The threshold for entering
problems into the corrective action program was
sufficiently low. Reviews of operating experience
information were comprehensive. In general, the
licensee properly prioritized items (by Action
Category) in its corrective action program
database, which ensured that timely resolution
and appropriate causal factor analyses were
employed commensurate with safety significance.
One exception involved a recent condition adverse
to quality in which the standby shutdown
facility's (SSF) diesel generator was unavailable
following the complete draining of radiator
coolant because of heater shell pin-hole leaks.
The licensee did not perform an in-depth root
cause analysis and thorough corrective actions
following its discovery of the degraded
condition. Also, for potential safety equipment
operability issues, the licensee did not always
conduct or document thorough evaluations of
present or past inoperability. Previous
non-compliance issues documented as non-cited
violations were properly tracked and resolved via
the corrective action program. The results of the
last comprehensive corrective action program
audit conducted by the licensee (September 1999)
were properly entered and dispositioned in the
corrective action program. Based on discussions
with plant personnel and the apparently low
threshold for items entered in the corrective
action program database, the inspectors concluded
that workers at the site generally felt free to
raise safety concerns to their management.
Inspection Report# : 2000010
Last modified :
May 03, 2001
This item appeared
in The Times & Free Press on Wednesday,
December 29, 1999.
NRC Urges TVA
Develop Better Plan For Ice Backup System at 2
N-Plants
By DAVE FLESSNER
Business Editor
Federal regulators
have given a cold shoulder to TVA's plan to
verify the amount of ice in an emergency backup
system at the Sequoyah and Watts Bar nuclear
power plants.
The Nuclear
Regulatory Commission has asked TVA to come up
with a better method of weighing the 3 million
pounds of ice in the containment walls at each
plant. The NRC's rejection this month of the
initial plan prolongs a troubling issue for TVA
and the other operators of the nine
Westinghouse-designed reactors that use ice
condensers as part of their safety systems.
Debris problems in
the condenser system at the Donald C. Cook
nuclear plant in Michigan helped force a 2-year
repair outage at that plant. A TVA whistleblower
made similar claims in 1995 at the Watts Bar
Nuclear Plant. Last year, a federal judge ordered
TVA to rehire Curtis Overall, who claimed he lost
his job for reporting that he found 200 screws
and fragments in the ice condensers at Watts Bar.
"Here we are
nearly five years after this issue surfaced at
Watts Bar and more than two years after the D.C.
Cook plant was shut down because of condenser
problems and TVA has still been unable to fix
this problem," said Jim Riccio, an attorney
for the Public Citizen's Critical Mass Energy
Project in Washington. "TVA is not meeting
plant regulations and even the NRC, which I think
has largely been taken over by the nuclear
industry, recognizes that."
TVA officials
insist that the ice condenser system is still
reliable in the unlikely event of an accident at
one of its reactors.
"We're going
to supply the NRC more information about what we
propose to be a part of the technical
specifications to monitor the performance of the
ice condensers," TVA spokeswoman Barbara
Martocci said.
Robert Martin, the
NRC project manager overseeing the review of the
ice condenser issue, said TVA and NRC officials
should meet next month to discuss the issue.
"We certainly
haven't found anything that calls us to shut down
any of these plants (with the ice
condensers)," he said.
The ice condenser
systems are designed to relieve pressure,
temperature and the possibility of a radioactive
release if a steam pipe breaks in a reactor
containment building. When the system works, the
steam hits the condenser ice and is turned to
water. The water is captured and never leaves the
building.
The ice condensers
allowed Westinghouse to design a smaller and less
expensive reactor containment building at its
pressurized water reactors.
TVA, Duke Power
Co. and Michigan Power Co. are the utilities that
own Westinghouse reactors that use ice
condensers. The utilities have formed an Ice
Condenser Mini Group to address concerns about
the reliability of the condensers. TVA is
responsible for developing technical
specifications to weigh the ice in the plants.
In a recent letter
to TVA, NRC project manager Ronald W. Hernan
rejected TVA's initial plan, claiming that nearly
half of the 1,994 ice baskets at Sequoyah can't
be adequately weighed under the proposed
surveillance plan.
The NRC continues
to give TVA high marks for the operation of its
nuclear plants overall, however. The Sequoyah
plant is part of a new pilot reporting system the
NRC launched this year and the plant is rated in
the top "green" category of all areas
of plant performance monitored by the NRC.
"TVA
continues to maintain all the systems in top
working order and we will work to address this
ice condenser issue," Ms. Martocci said.
"We are very comfortable in saying that we
believe our plants will operate as
designed."
|